摘要
为了满足液流深部转向而自行研制了深部液流转向剂ZYTQ01,并在濮城油田南区沙二上2+3油藏开展了调驱先导试验。介绍了ZYTQ01的深调机理和驱油机理,对其性能(包括注入水对ZYTQ01膨胀度的影响、流动压力与流量的关系、纵向调剖效果、改善平面波及效果、微观驱油效果)进行了试验评价。现场试验结果表明,采用ZYTQ01调驱工艺进行治理后,凝胶颗粒在地层深部调剖成功,使受益油井增油降水效果显著。
A in-depth fluid flowing diverting agent ZYTQ01 is developed by ourselves to meet the needs of fluid flowing diverting in deep zone, by which in-depth adjustment and oil displacement pilot test is performed in Reservoir 2 + 3 in the upper member of Es3 of south region in Pucheng Oilfield, the in-depth adjustment and displacement mechanisms are introduced. Experimental evaluation is made on its performance (including the effect of injected water on the degree of expan- sion, the correlation between pressure and flowrate. vertical profile controlling result, improving the areal sweep efficiency and micro-displacement efficiency). The result of field testing shows that after the treatment is made with ZYTQ01 displacement process , in the in-depth reservoir profile control, the gelling particles are successfully used, with evident oil production increase and water reduction.
出处
《江汉石油学院学报》
EI
CSCD
北大核心
2003年第2期95-96,共2页
Journal of Jianghan Petroleum Institute
关键词
提高采收率
流动调整荆
驱油剂
驱油机理
先导性试验
濮城油田
enhanced oil recovery
flowing adjustment agent
displacement agent
displacement mechanism
pilot test
Pucheng Oilfield