摘要
KL2-H1井是西气东输2007年在克拉区块的一口水平井。该井三开段为高压盐膏层,四开段为白云岩高压气层;钻井液密度为2.00~2.25g/cm2,压井液密度为2.40g/cm2,使用混10%~15%原油基液,固相含量相对高,且容量限低,同时由于带POWVER或MWD定向工具钻进,只能使用重晶石加重,使得钻井液的流变性较差,现场施工困难。经过室内实验,研究出了一套适用于现场要求和用重晶石加重的流变性较好的高密度饱和盐水钻井液和压井液配方。现场应用表明,该钻井液的各项性能均能很好地满足钻进要求。
Well KL2-H1 is a horizontal well located in Block Kela for the West-East natural gas transmission project.The third interval of this well penetrated a high pressure salt/gypsum formation and the fourth penetrated a high pressure dolomitic gas bearing zone.The density of the saltwater drilling fluid used was 2.00~2.25 g/cm3,weighted only with barite because of the use of POWVER/MWD in drilling operation,and the kill mud had a density of 2.40 g/cm3.The mud also had 10%~15% oil mixed in it.Bad rheology of the mud made field operation very tough.The drilling fluid and kill mud were then changed to a high density saturated saltwater fluids that were weighted with barite.Laboratory experiment and field application results showed that the drilling fluid and the kill mud met the requirements of filed operation.
出处
《钻井液与完井液》
CAS
2009年第4期26-28,共3页
Drilling Fluid & Completion Fluid
关键词
水平井
高密度钻井液
饱和盐水钻井液
钻井液配方
流变性
Horizontal well
High density drilling fluid
Saturated saltwater drilling fluid
Drilling fluid formulation
Rheology
作者简介
第一作者简介:张欢庆,工程师,1971年生,1996年毕业于承德石油高等专科学校分析专业,一直从事钻井液的室内研究及现场技术服务。地址:新疆库尔勒塔里木油田建设有限公司泥浆工程部;邮政编码841000;电话(0996)2174100。