A nonlinear robust controller was presented to improve the tracking control performance of a flexible air-breathing hypersonic vehicle(AHV) which is subjected to system parametric uncertainties and unknown additive ti...A nonlinear robust controller was presented to improve the tracking control performance of a flexible air-breathing hypersonic vehicle(AHV) which is subjected to system parametric uncertainties and unknown additive time-varying disturbances.The longitudinal dynamic model for the flexible AHV was used for the control development.High-gain observers were designed to compensate for the system uncertainties and additive disturbances.Small gain theorem and Lyapunov based stability analysis were utilized to prove the stability of the closed loop system.Locally uniformly ultimately bounded tracking of the vehicle's velocity,altitude and attack angle were achieved under aeroelastic effects,system parametric uncertainties and unknown additive disturbances.Matlab/Simulink simulation results were provided to validate the robustness of the proposed control design.The simulation results demonstrate that the tracking errors stay in a small region around zero.展开更多
In order to explore the precise dynamic response of the maglev train and verify the validity of proposed controller,a maglev guideway-electromagnet-air spring-cabin coupled model is developed in the first step.Based o...In order to explore the precise dynamic response of the maglev train and verify the validity of proposed controller,a maglev guideway-electromagnet-air spring-cabin coupled model is developed in the first step.Based on the coupled model,the stresses of the modules are analyzed,and it is pointed out that the inherent nonlinearity,the inner coupling,misalignments between the sensors and actuators,and external disturbances are the main issues that should be considered for the maglev engineering.Furthermore,a feedback linearization controller based on the mathematical model of a maglev module is derived,in which the nonlinearity,coupling and misalignments are taken into account.Then,to attenuate the effect of external disturbances,a disturbance observer is proposed and the dynamics of the estimation error is analyzed using the input-to-state stability theory.It shows that the error is negligible under a low-frequency disturbance.However,at the high-frequency range,the error is unacceptable and the disturbances can not be compensated in time,which lead to over designed fluctuations of levitation gap,even a clash between the upper surface of electromagnet and lower surface of guideway.To solve this problem,a novel nonlinear acceleration feedback is put forward to enhancing the attenuation ability of fast varying disturbances.Finally,numerical comparisons show that the proposed controller outperforms the traditional feedback linearization controller and maintains good robustness under disturbances.展开更多
基金Projects(90916004,60804004)supported by the National Natural Science Foundation of ChinaProject supported by the Program for the New Century,ChinaProject(NCET-09-0590)supported by Excellent Talents in University,China
文摘A nonlinear robust controller was presented to improve the tracking control performance of a flexible air-breathing hypersonic vehicle(AHV) which is subjected to system parametric uncertainties and unknown additive time-varying disturbances.The longitudinal dynamic model for the flexible AHV was used for the control development.High-gain observers were designed to compensate for the system uncertainties and additive disturbances.Small gain theorem and Lyapunov based stability analysis were utilized to prove the stability of the closed loop system.Locally uniformly ultimately bounded tracking of the vehicle's velocity,altitude and attack angle were achieved under aeroelastic effects,system parametric uncertainties and unknown additive disturbances.Matlab/Simulink simulation results were provided to validate the robustness of the proposed control design.The simulation results demonstrate that the tracking errors stay in a small region around zero.
基金Project(60404003)supported by the National Natural Science Foundation of China
文摘In order to explore the precise dynamic response of the maglev train and verify the validity of proposed controller,a maglev guideway-electromagnet-air spring-cabin coupled model is developed in the first step.Based on the coupled model,the stresses of the modules are analyzed,and it is pointed out that the inherent nonlinearity,the inner coupling,misalignments between the sensors and actuators,and external disturbances are the main issues that should be considered for the maglev engineering.Furthermore,a feedback linearization controller based on the mathematical model of a maglev module is derived,in which the nonlinearity,coupling and misalignments are taken into account.Then,to attenuate the effect of external disturbances,a disturbance observer is proposed and the dynamics of the estimation error is analyzed using the input-to-state stability theory.It shows that the error is negligible under a low-frequency disturbance.However,at the high-frequency range,the error is unacceptable and the disturbances can not be compensated in time,which lead to over designed fluctuations of levitation gap,even a clash between the upper surface of electromagnet and lower surface of guideway.To solve this problem,a novel nonlinear acceleration feedback is put forward to enhancing the attenuation ability of fast varying disturbances.Finally,numerical comparisons show that the proposed controller outperforms the traditional feedback linearization controller and maintains good robustness under disturbances.