Drum level sloshing is the latest discovery in the application of heat recovery steam generator (HRSG) in combined cycle, and shows certain negative influence on drum level controlling. In order to improve drum level ...Drum level sloshing is the latest discovery in the application of heat recovery steam generator (HRSG) in combined cycle, and shows certain negative influence on drum level controlling. In order to improve drum level controlling, influence factors on the drum level sloshing were investigated. Firstly, drum sub-modules were developed using the method of modularization modeling, and then the model of drum level sloshing was set up as well. Experiments were carried out on the experimental rig, and the model was validated using the obtained experimental results. Dynamic simulation was made based on the model to get a 3-D graph of drum level sloshing, which shows a vivid procedure of drum level sloshing. The effect of feed-water flow rate, main-steam flow rate and heating quantity on the drum level sloshing was analyzed. The simulation results indicate that the signals with frequency higher than 0.05 Hz are that of drum level sloshing, the signals with frequency of 0.0-0.05 Hz are that of drum level trendy and "false water level", and variation of the feed-water flow rates, main-steam flow rates and heating quantities can change the frequency of drum level sloshing, i.e., the frequency of sloshing increases with the increase of feed-water flow rate, or the decrease of the main-steam flow rate and the heating quantity. This research work is fundamental to improve signal-to-noise ratio of drum level signal and precise controlling of drum level.展开更多
The performance of a patented water pumping model with steam-air power was presented, which operates automatically by direct contact cooling method. The main objective was to study feasibility of a pumping model for u...The performance of a patented water pumping model with steam-air power was presented, which operates automatically by direct contact cooling method. The main objective was to study feasibility of a pumping model for underground water. In this model, a heater installed within the heat tank represented sources of waste heat as energy input for finding appropriate conditions of the 10 L pump model. The system operation had five stages: heating, pumping, vapor flow, cooling, and water suction. The overall water heads of 3, 4.5, 6 and 7.5 m were tested. At the same time, it was found that the pump with 50% air volume is sufficient for pumping water to a desired level. In the experiment, the temperatures in the heating and pumping stages were 100-103 ℃and 80-90 ℃, respectively. The pressure in the pumping stage was 12-18 kPa, and the pressure in the suction stage was about-80 kPa, sufficient for the best performance. It could pump 170 L of water at a 2 m suction head, 120 L at a 3.5 m suction head, 100 L at a 5 m suction head, and 65 L at a 6.5 m suction head in 2 h. A mathematical model for larger pumps was also presented, which operates nearly the same as the present system. Economic analysis of the 10 L pump was also included.展开更多
基金Project(51276023) supported by the National Natural Science Foundation of ChinaProject(09k069) supported by the Open Project Funded by Universities Innovation Platform, Hunan Province, ChinaProject(2011GK311) supported by the Office of Science and Technology of Hunan Province, China
文摘Drum level sloshing is the latest discovery in the application of heat recovery steam generator (HRSG) in combined cycle, and shows certain negative influence on drum level controlling. In order to improve drum level controlling, influence factors on the drum level sloshing were investigated. Firstly, drum sub-modules were developed using the method of modularization modeling, and then the model of drum level sloshing was set up as well. Experiments were carried out on the experimental rig, and the model was validated using the obtained experimental results. Dynamic simulation was made based on the model to get a 3-D graph of drum level sloshing, which shows a vivid procedure of drum level sloshing. The effect of feed-water flow rate, main-steam flow rate and heating quantity on the drum level sloshing was analyzed. The simulation results indicate that the signals with frequency higher than 0.05 Hz are that of drum level sloshing, the signals with frequency of 0.0-0.05 Hz are that of drum level trendy and "false water level", and variation of the feed-water flow rates, main-steam flow rates and heating quantities can change the frequency of drum level sloshing, i.e., the frequency of sloshing increases with the increase of feed-water flow rate, or the decrease of the main-steam flow rate and the heating quantity. This research work is fundamental to improve signal-to-noise ratio of drum level signal and precise controlling of drum level.
基金the financial support provided by National Research Council of Thailand and the Energy Technology Division, School of Energy Environment and Materials, King Mongkut’s University of Technology Thonburisupported by the Higher Education Research Promotion and National Research University Project of Thailand, Office of the Higher Education Commission
文摘The performance of a patented water pumping model with steam-air power was presented, which operates automatically by direct contact cooling method. The main objective was to study feasibility of a pumping model for underground water. In this model, a heater installed within the heat tank represented sources of waste heat as energy input for finding appropriate conditions of the 10 L pump model. The system operation had five stages: heating, pumping, vapor flow, cooling, and water suction. The overall water heads of 3, 4.5, 6 and 7.5 m were tested. At the same time, it was found that the pump with 50% air volume is sufficient for pumping water to a desired level. In the experiment, the temperatures in the heating and pumping stages were 100-103 ℃and 80-90 ℃, respectively. The pressure in the pumping stage was 12-18 kPa, and the pressure in the suction stage was about-80 kPa, sufficient for the best performance. It could pump 170 L of water at a 2 m suction head, 120 L at a 3.5 m suction head, 100 L at a 5 m suction head, and 65 L at a 6.5 m suction head in 2 h. A mathematical model for larger pumps was also presented, which operates nearly the same as the present system. Economic analysis of the 10 L pump was also included.