Geological adaptability matching design of a disc cutter is the prerequisite of cutter head design for tunnel boring machines(TBMs)and plays an important role in improving the tunneling efficiency of TBMs.The main pur...Geological adaptability matching design of a disc cutter is the prerequisite of cutter head design for tunnel boring machines(TBMs)and plays an important role in improving the tunneling efficiency of TBMs.The main purpose of the cutter matching design is to evaluate the cutter performance and select the appropriate cutter size.In this paper,a novel evaluation method based on multicriteria decision making(MCDM)techniques was developed to help TBM designers in the process of determining the cutter size.The analytic hierarchy process(AHP)and matter element analysis were applied to obtaining the weights of the cutter evaluation criteria,and the fuzzy comprehensive evaluation and technique for order performance by similarity to ideal solution(TOPSIS)approaches were employed to determine the ranking of the cutters.A case application was offered to illustrate and validate the proposed method.The results of the project case demonstrate that this method is reasonable and feasible for disc cutter size selection in cutter head design.展开更多
To enhance machining efficiency,tool change time has to be reduced.Thus,for an automatic tool changer attached to a machining center,the tool change time is to be reduced.Also the automatic tool changer is a main part...To enhance machining efficiency,tool change time has to be reduced.Thus,for an automatic tool changer attached to a machining center,the tool change time is to be reduced.Also the automatic tool changer is a main part of the machining center as a driving source.The static attributes of the automatic tool changer using the commercial code,ANSYS Workbench V12,were tried to interpret.And the optimum design of automatic tool changer arm was proposed by performing the multi-stage optimum design.The shape optimization of the automatic tool changer was proposed and the result was verified to obtain acceptable improvements.It is possible to obtain an optimized model in which the maximum deformation,maximum stress,and mass are reduced by 10.46%,12.89% and 9.26%,respectively,compared with those of the initial model.Also,the results between conventional method by the design of experiments and proposed method by the multi-stage optimum design method were compared.展开更多
As the sampling rates of the inner loop and the outer loop of the target tracking control system are different,a typical digital multi-rate control system was formed.If the traditional single-rate design method was ap...As the sampling rates of the inner loop and the outer loop of the target tracking control system are different,a typical digital multi-rate control system was formed.If the traditional single-rate design method was applied,the low sampling rate loop will seriously impact the dynamical characteristic of the system.After analyzing and calculating the impact law of the low sampling rate loop to the bandwidth and the stability of the tracking system,a kind of multi-rate control system design method was introduced.Corresponding to the different sampling rates of the inner loop and the outer loop,the multi-rate control strategy was constituted by a high sampling rate sub-controller and a low sampling rate sub-controller.The two sub-controllers were designed separately and connected by means of the sampling rate converter.The low sampling rate controller determined the response rapidity of the system,while the high sampling rate controller applied additionally effective control outputs to the system during a sampling interval of the low sampling rate controller.With the introduced high and low sampling rates sub-controllers,the tracking control system can achieve the same performance as a single-rate controller with high sampling rate,yet it works under a much lower sampling rate.The simulation and experimental results show the effectiveness of the introduced multi-rate control design method.It reduces the settling time by 5 times and the over shoot by 4 times compared with the PID control.展开更多
基金Project(51475478)supported by the National Natural Science Foundation of ChinaProject(2013CB035401)supported by the National Basic Research Program of China+1 种基金Project(2012AA041801)supported by the National High-tech Research and Development Program of ChinaProject(CX2014B058)supported by the Hunan Provincial Innovation Foundation for Postgraduate,China
文摘Geological adaptability matching design of a disc cutter is the prerequisite of cutter head design for tunnel boring machines(TBMs)and plays an important role in improving the tunneling efficiency of TBMs.The main purpose of the cutter matching design is to evaluate the cutter performance and select the appropriate cutter size.In this paper,a novel evaluation method based on multicriteria decision making(MCDM)techniques was developed to help TBM designers in the process of determining the cutter size.The analytic hierarchy process(AHP)and matter element analysis were applied to obtaining the weights of the cutter evaluation criteria,and the fuzzy comprehensive evaluation and technique for order performance by similarity to ideal solution(TOPSIS)approaches were employed to determine the ranking of the cutters.A case application was offered to illustrate and validate the proposed method.The results of the project case demonstrate that this method is reasonable and feasible for disc cutter size selection in cutter head design.
基金Work(RTI04-01-03) supported by Grant from Regional Technology Innovation Program of the Ministry of Knowledge Economy (MKE),Korea
文摘To enhance machining efficiency,tool change time has to be reduced.Thus,for an automatic tool changer attached to a machining center,the tool change time is to be reduced.Also the automatic tool changer is a main part of the machining center as a driving source.The static attributes of the automatic tool changer using the commercial code,ANSYS Workbench V12,were tried to interpret.And the optimum design of automatic tool changer arm was proposed by performing the multi-stage optimum design.The shape optimization of the automatic tool changer was proposed and the result was verified to obtain acceptable improvements.It is possible to obtain an optimized model in which the maximum deformation,maximum stress,and mass are reduced by 10.46%,12.89% and 9.26%,respectively,compared with those of the initial model.Also,the results between conventional method by the design of experiments and proposed method by the multi-stage optimum design method were compared.
基金Project(51105372) supported by the National Natural Science Foundation of ChinaProject(JC12-03-01) supported by the Research Plan of National University of Defense Technology,China
文摘As the sampling rates of the inner loop and the outer loop of the target tracking control system are different,a typical digital multi-rate control system was formed.If the traditional single-rate design method was applied,the low sampling rate loop will seriously impact the dynamical characteristic of the system.After analyzing and calculating the impact law of the low sampling rate loop to the bandwidth and the stability of the tracking system,a kind of multi-rate control system design method was introduced.Corresponding to the different sampling rates of the inner loop and the outer loop,the multi-rate control strategy was constituted by a high sampling rate sub-controller and a low sampling rate sub-controller.The two sub-controllers were designed separately and connected by means of the sampling rate converter.The low sampling rate controller determined the response rapidity of the system,while the high sampling rate controller applied additionally effective control outputs to the system during a sampling interval of the low sampling rate controller.With the introduced high and low sampling rates sub-controllers,the tracking control system can achieve the same performance as a single-rate controller with high sampling rate,yet it works under a much lower sampling rate.The simulation and experimental results show the effectiveness of the introduced multi-rate control design method.It reduces the settling time by 5 times and the over shoot by 4 times compared with the PID control.